Decrease Sucrose Loss through Blackstrap

Detalhes bibliográficos
Autor(a) principal: Martins, Alexandra Sofia da Silva
Data de Publicação: 2019
Tipo de documento: Dissertação
Idioma: eng
Título da fonte: Repositórios Científicos de Acesso Aberto de Portugal (RCAAP)
Texto Completo: http://hdl.handle.net/10362/89167
Resumo: ´To reduce the chemical inversion of sucrose, and consequently increase the profit margin, many refineries are trying to optimise their production process by focusing on the areas most prone to losses. A Pareto diagram is developed every fiscal year to help understand the areas that have a higher contribution to this problem. In the year FY18 (October of 2017 to October of 2018) it was realised that recovery represented about 16% of the total chemical losses. Thus, before making any alterations, the different boiling pans had to be characterised, as well as its inlet and outlet streams and respective centrifuges. Since there was no time to define all of them, the present work focused on the A1 and A pans. After setting these parameters, improvements to the crystallisation profiles were proposed. Through the alteration of the absolute pressure, temperature, Brix, and tons of fed syrup, some positive changes could be observed. Using Hypothesis Tests, one for each boiling pan, the new invert generation was deter-mined with a confidence level of 90%. In A1 there was an invert reduction of 3.32 percentual points (from 8.62% to 5.30%), while for A 3.27 (from 6.31% to 3.04%). By analysing the control chart of the final molasses of recovery, it was proved that this decrease occurred and it was 0.02%. Monetarily, this value corresponds approximately to the estimated profit projection for the new invert generation. One of the goals of this thesis was also to increase the process yield. However, this value has not changed. Lastly, the centrifuges wash time was optimised, with the assistance of Design of Experi-ments (DOE). Thus, through some tests, it was possible to determine the optimal wash time to reduce the presence of ash and invert in the purged sugar. When separated from the syrup, this sugar returns into the process. In the A1 centrifugal, by applying an eight seconds wash, there was a reduction in inverts and ashes of -36.59% and -35.84%, respectively. As for the A centrif-ugal, a first wash of six seconds, followed by one of ten seconds, reduced the inverts by -62.58% and the ashes by -61.65%.
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spelling Decrease Sucrose Loss through BlackstrapSucroseChemical LossesBoiling panCentrifugesInvertsAshesDomínio/Área Científica::Engenharia e Tecnologia::Engenharia Química´To reduce the chemical inversion of sucrose, and consequently increase the profit margin, many refineries are trying to optimise their production process by focusing on the areas most prone to losses. A Pareto diagram is developed every fiscal year to help understand the areas that have a higher contribution to this problem. In the year FY18 (October of 2017 to October of 2018) it was realised that recovery represented about 16% of the total chemical losses. Thus, before making any alterations, the different boiling pans had to be characterised, as well as its inlet and outlet streams and respective centrifuges. Since there was no time to define all of them, the present work focused on the A1 and A pans. After setting these parameters, improvements to the crystallisation profiles were proposed. Through the alteration of the absolute pressure, temperature, Brix, and tons of fed syrup, some positive changes could be observed. Using Hypothesis Tests, one for each boiling pan, the new invert generation was deter-mined with a confidence level of 90%. In A1 there was an invert reduction of 3.32 percentual points (from 8.62% to 5.30%), while for A 3.27 (from 6.31% to 3.04%). By analysing the control chart of the final molasses of recovery, it was proved that this decrease occurred and it was 0.02%. Monetarily, this value corresponds approximately to the estimated profit projection for the new invert generation. One of the goals of this thesis was also to increase the process yield. However, this value has not changed. Lastly, the centrifuges wash time was optimised, with the assistance of Design of Experi-ments (DOE). Thus, through some tests, it was possible to determine the optimal wash time to reduce the presence of ash and invert in the purged sugar. When separated from the syrup, this sugar returns into the process. In the A1 centrifugal, by applying an eight seconds wash, there was a reduction in inverts and ashes of -36.59% and -35.84%, respectively. As for the A centrif-ugal, a first wash of six seconds, followed by one of ten seconds, reduced the inverts by -62.58% and the ashes by -61.65%.Ribeiro, JoaquimEusébio, MárioRUNMartins, Alexandra Sofia da Silva2022-09-23T00:30:52Z2019-11-2920192019-11-29T00:00:00Zinfo:eu-repo/semantics/publishedVersioninfo:eu-repo/semantics/masterThesisapplication/pdfhttp://hdl.handle.net/10362/89167enginfo:eu-repo/semantics/openAccessreponame:Repositórios Científicos de Acesso Aberto de Portugal (RCAAP)instname:FCCN, serviços digitais da FCT – Fundação para a Ciência e a Tecnologiainstacron:RCAAP2024-05-22T17:42:26Zoai:run.unl.pt:10362/89167Portal AgregadorONGhttps://www.rcaap.pt/oai/openaireinfo@rcaap.ptopendoar:https://opendoar.ac.uk/repository/71602025-05-28T17:13:43.442008Repositórios Científicos de Acesso Aberto de Portugal (RCAAP) - FCCN, serviços digitais da FCT – Fundação para a Ciência e a Tecnologiafalse
dc.title.none.fl_str_mv Decrease Sucrose Loss through Blackstrap
title Decrease Sucrose Loss through Blackstrap
spellingShingle Decrease Sucrose Loss through Blackstrap
Martins, Alexandra Sofia da Silva
Sucrose
Chemical Losses
Boiling pan
Centrifuges
Inverts
Ashes
Domínio/Área Científica::Engenharia e Tecnologia::Engenharia Química
title_short Decrease Sucrose Loss through Blackstrap
title_full Decrease Sucrose Loss through Blackstrap
title_fullStr Decrease Sucrose Loss through Blackstrap
title_full_unstemmed Decrease Sucrose Loss through Blackstrap
title_sort Decrease Sucrose Loss through Blackstrap
author Martins, Alexandra Sofia da Silva
author_facet Martins, Alexandra Sofia da Silva
author_role author
dc.contributor.none.fl_str_mv Ribeiro, Joaquim
Eusébio, Mário
RUN
dc.contributor.author.fl_str_mv Martins, Alexandra Sofia da Silva
dc.subject.por.fl_str_mv Sucrose
Chemical Losses
Boiling pan
Centrifuges
Inverts
Ashes
Domínio/Área Científica::Engenharia e Tecnologia::Engenharia Química
topic Sucrose
Chemical Losses
Boiling pan
Centrifuges
Inverts
Ashes
Domínio/Área Científica::Engenharia e Tecnologia::Engenharia Química
description ´To reduce the chemical inversion of sucrose, and consequently increase the profit margin, many refineries are trying to optimise their production process by focusing on the areas most prone to losses. A Pareto diagram is developed every fiscal year to help understand the areas that have a higher contribution to this problem. In the year FY18 (October of 2017 to October of 2018) it was realised that recovery represented about 16% of the total chemical losses. Thus, before making any alterations, the different boiling pans had to be characterised, as well as its inlet and outlet streams and respective centrifuges. Since there was no time to define all of them, the present work focused on the A1 and A pans. After setting these parameters, improvements to the crystallisation profiles were proposed. Through the alteration of the absolute pressure, temperature, Brix, and tons of fed syrup, some positive changes could be observed. Using Hypothesis Tests, one for each boiling pan, the new invert generation was deter-mined with a confidence level of 90%. In A1 there was an invert reduction of 3.32 percentual points (from 8.62% to 5.30%), while for A 3.27 (from 6.31% to 3.04%). By analysing the control chart of the final molasses of recovery, it was proved that this decrease occurred and it was 0.02%. Monetarily, this value corresponds approximately to the estimated profit projection for the new invert generation. One of the goals of this thesis was also to increase the process yield. However, this value has not changed. Lastly, the centrifuges wash time was optimised, with the assistance of Design of Experi-ments (DOE). Thus, through some tests, it was possible to determine the optimal wash time to reduce the presence of ash and invert in the purged sugar. When separated from the syrup, this sugar returns into the process. In the A1 centrifugal, by applying an eight seconds wash, there was a reduction in inverts and ashes of -36.59% and -35.84%, respectively. As for the A centrif-ugal, a first wash of six seconds, followed by one of ten seconds, reduced the inverts by -62.58% and the ashes by -61.65%.
publishDate 2019
dc.date.none.fl_str_mv 2019-11-29
2019
2019-11-29T00:00:00Z
2022-09-23T00:30:52Z
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