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Productivity improvement in a company of the industry of bolting systems

Bibliographic Details
Main Author: Oliveira, Jorge Miguel Porfírio
Publication Date: 2021
Format: Master thesis
Language: eng
Source: Repositórios Científicos de Acesso Aberto de Portugal (RCAAP)
Download full: http://hdl.handle.net/10400.22/20147
Summary: Nowadays, the companies face an extreme need of having high levels of productivity (P) in order to survive in the market`s competition. In this context, this work was performed in the production department of alki Technik GmbH, a company that operates in the field of bolting systems, making production of tools in a make-to-order (MTO) basis, and services as well. The work had the main aims of measurement of the production performance in terms of its P level and establishment of strategies to reach its improvement. The first phase of the work was focused in obtaining the necessary elements to measure the real levels of P in a weekly basis, which are the inputs (IN) in terms of time capacity and the outputs (OUT) in terms of time with production of tools and execution of services. After found ways to properly quantify IN and OUT, the P started to be observed and after the first three weeks, the observed Ps were considered too low for what the company needs, and it was also confirmed when compared with P levels presented in another studies. Some improvement methods were implemented, such as, a Visual Management (VM) method, which consisted in establishing each Friday a map with a work plan for the following week and placing it in the workshop, and Kaizen philosophy in terms of asking the employees about activities of their daily work that they considered that could be optimized to proceed with its analysis as Kaizen Optimizations (KOs), in order to find optimization solutions. A total of six KOs were proposed, being the time saving estimate of 101 hours per year. One of the KOs was immediate implemented, as well as the VM method, and the following three weeks showed P improvement, with the observed indexes of 59,2%, 52,1% and 58,3% respectively, when on previous weeks the highest observed value had been 43,7%. Finally, it was made the analysis of the workshop`s layout, as facility layouts play also a huge role in the productive performance, through the Systematic Layout Planning (SLP) method in order optimize the flows. From this analysis, two optimization alternatives (OAs) were designed. OA1, where a few changes are proposed without extra costs have been estimated a cost reduction with flows of 5,94% OA2, where some further changes are proposed, being in this case the estimated costs reduction with flows of 20,3%. However, this last OA would carry costs of its implementation. The conclusions highlight the P improvement achieved through this work. Further improvement was left through the KOsfor the process and OAsfor the workshop layout.
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spelling Productivity improvement in a company of the industry of bolting systemsProductivity ImprovementPlanningProduction OptimizationKaizenVisual ManagementFacility Layout OptimizationSystematic Layout PlanningMelhoria da ProdutividadePlaneamentoOptimização da ProduçãoGestão VisualOptimização do layout da instalaçãoNowadays, the companies face an extreme need of having high levels of productivity (P) in order to survive in the market`s competition. In this context, this work was performed in the production department of alki Technik GmbH, a company that operates in the field of bolting systems, making production of tools in a make-to-order (MTO) basis, and services as well. The work had the main aims of measurement of the production performance in terms of its P level and establishment of strategies to reach its improvement. The first phase of the work was focused in obtaining the necessary elements to measure the real levels of P in a weekly basis, which are the inputs (IN) in terms of time capacity and the outputs (OUT) in terms of time with production of tools and execution of services. After found ways to properly quantify IN and OUT, the P started to be observed and after the first three weeks, the observed Ps were considered too low for what the company needs, and it was also confirmed when compared with P levels presented in another studies. Some improvement methods were implemented, such as, a Visual Management (VM) method, which consisted in establishing each Friday a map with a work plan for the following week and placing it in the workshop, and Kaizen philosophy in terms of asking the employees about activities of their daily work that they considered that could be optimized to proceed with its analysis as Kaizen Optimizations (KOs), in order to find optimization solutions. A total of six KOs were proposed, being the time saving estimate of 101 hours per year. One of the KOs was immediate implemented, as well as the VM method, and the following three weeks showed P improvement, with the observed indexes of 59,2%, 52,1% and 58,3% respectively, when on previous weeks the highest observed value had been 43,7%. Finally, it was made the analysis of the workshop`s layout, as facility layouts play also a huge role in the productive performance, through the Systematic Layout Planning (SLP) method in order optimize the flows. From this analysis, two optimization alternatives (OAs) were designed. OA1, where a few changes are proposed without extra costs have been estimated a cost reduction with flows of 5,94% OA2, where some further changes are proposed, being in this case the estimated costs reduction with flows of 20,3%. However, this last OA would carry costs of its implementation. The conclusions highlight the P improvement achieved through this work. Further improvement was left through the KOsfor the process and OAsfor the workshop layout.Silva, Francisco José Gomes daREPOSITÓRIO P.PORTOOliveira, Jorge Miguel Porfírio2022-03-07T15:12:34Z20212021-01-01T00:00:00Zinfo:eu-repo/semantics/publishedVersioninfo:eu-repo/semantics/masterThesisapplication/pdftext/plain; charset=utf-8http://hdl.handle.net/10400.22/20147urn:tid:202937240enginfo:eu-repo/semantics/openAccessreponame:Repositórios Científicos de Acesso Aberto de Portugal (RCAAP)instname:FCCN, serviços digitais da FCT – Fundação para a Ciência e a Tecnologiainstacron:RCAAP2025-03-07T10:20:24Zoai:recipp.ipp.pt:10400.22/20147Portal AgregadorONGhttps://www.rcaap.pt/oai/openaireinfo@rcaap.ptopendoar:https://opendoar.ac.uk/repository/71602025-05-29T00:49:05.664322Repositórios Científicos de Acesso Aberto de Portugal (RCAAP) - FCCN, serviços digitais da FCT – Fundação para a Ciência e a Tecnologiafalse
dc.title.none.fl_str_mv Productivity improvement in a company of the industry of bolting systems
title Productivity improvement in a company of the industry of bolting systems
spellingShingle Productivity improvement in a company of the industry of bolting systems
Oliveira, Jorge Miguel Porfírio
Productivity Improvement
Planning
Production Optimization
Kaizen
Visual Management
Facility Layout Optimization
Systematic Layout Planning
Melhoria da Produtividade
Planeamento
Optimização da Produção
Gestão Visual
Optimização do layout da instalação
title_short Productivity improvement in a company of the industry of bolting systems
title_full Productivity improvement in a company of the industry of bolting systems
title_fullStr Productivity improvement in a company of the industry of bolting systems
title_full_unstemmed Productivity improvement in a company of the industry of bolting systems
title_sort Productivity improvement in a company of the industry of bolting systems
author Oliveira, Jorge Miguel Porfírio
author_facet Oliveira, Jorge Miguel Porfírio
author_role author
dc.contributor.none.fl_str_mv Silva, Francisco José Gomes da
REPOSITÓRIO P.PORTO
dc.contributor.author.fl_str_mv Oliveira, Jorge Miguel Porfírio
dc.subject.por.fl_str_mv Productivity Improvement
Planning
Production Optimization
Kaizen
Visual Management
Facility Layout Optimization
Systematic Layout Planning
Melhoria da Produtividade
Planeamento
Optimização da Produção
Gestão Visual
Optimização do layout da instalação
topic Productivity Improvement
Planning
Production Optimization
Kaizen
Visual Management
Facility Layout Optimization
Systematic Layout Planning
Melhoria da Produtividade
Planeamento
Optimização da Produção
Gestão Visual
Optimização do layout da instalação
description Nowadays, the companies face an extreme need of having high levels of productivity (P) in order to survive in the market`s competition. In this context, this work was performed in the production department of alki Technik GmbH, a company that operates in the field of bolting systems, making production of tools in a make-to-order (MTO) basis, and services as well. The work had the main aims of measurement of the production performance in terms of its P level and establishment of strategies to reach its improvement. The first phase of the work was focused in obtaining the necessary elements to measure the real levels of P in a weekly basis, which are the inputs (IN) in terms of time capacity and the outputs (OUT) in terms of time with production of tools and execution of services. After found ways to properly quantify IN and OUT, the P started to be observed and after the first three weeks, the observed Ps were considered too low for what the company needs, and it was also confirmed when compared with P levels presented in another studies. Some improvement methods were implemented, such as, a Visual Management (VM) method, which consisted in establishing each Friday a map with a work plan for the following week and placing it in the workshop, and Kaizen philosophy in terms of asking the employees about activities of their daily work that they considered that could be optimized to proceed with its analysis as Kaizen Optimizations (KOs), in order to find optimization solutions. A total of six KOs were proposed, being the time saving estimate of 101 hours per year. One of the KOs was immediate implemented, as well as the VM method, and the following three weeks showed P improvement, with the observed indexes of 59,2%, 52,1% and 58,3% respectively, when on previous weeks the highest observed value had been 43,7%. Finally, it was made the analysis of the workshop`s layout, as facility layouts play also a huge role in the productive performance, through the Systematic Layout Planning (SLP) method in order optimize the flows. From this analysis, two optimization alternatives (OAs) were designed. OA1, where a few changes are proposed without extra costs have been estimated a cost reduction with flows of 5,94% OA2, where some further changes are proposed, being in this case the estimated costs reduction with flows of 20,3%. However, this last OA would carry costs of its implementation. The conclusions highlight the P improvement achieved through this work. Further improvement was left through the KOsfor the process and OAsfor the workshop layout.
publishDate 2021
dc.date.none.fl_str_mv 2021
2021-01-01T00:00:00Z
2022-03-07T15:12:34Z
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